CONTROL AND MODELLING IN EXTRACTION METALLURGY
Copyright (c) IFAC Automation in Mining, Mineral and Metal Processing, Helsinki , Finland, 1983
THE QUALITY CONTROL SYSTEM OF SINTERING PLANT AT KASHIMA STEEL WORKS O. Arai*, A. Yamamoto*, T. Joko**, K. Inada*** and S. Yumoto**** *Instrumentation and Control Engineering Section, Kashima Steel Works, Sumitomo Metal Industries, Ltd., Ibarakz; 314 Japan **Iron-making Control Sectl'on, Kashima Steel Works, Sumitomo Metal Industries, Ltd., Ibaraki, 314 Japan ***Instrumentation and Control Technology Department, Central Research Laboratory, Sumitomo Metal Industries, Ltd., Hyogo, 660 Japan ****System Planning Department, Kahima Steel Works, Sumitomo Metal Industries, Ltd., Ibaraki, 314 Japan
Abstract In recent years, the quality control of sintered ore has become more and more important for stable operation of modern blast furnaces where the sinter ratio of feedstock material exceeds 50%. The quality control system of sintering plant has been developed by SMI (Sumitomo Metal Industries, Ltd.), which consists of the measurement systems of free carbon and FeO content in raw mat erials , the control system of particle distribution of crushed coke and the FeO content in sintered ore. It's well known that the conventional batch sampling method has such limitations for quality control of sintered ore as its poor sampling frequency and time lag before result is acquired. In the past several years, SMI has developed the sensors and control system of sintered ore with satisfactory results. Our research in those several years, the following result s are attained. (1) There is close relation between indices of RDI (Reduction and Dis integration Index) and TI (Tumbler Index) of sintered products and the ratio of smaller particle size of crushed coke than 1 mm. (2) FeO con tent of products is con tr ollable by regulating the coke ratio in relation to the FeO content of raw materials and products. (3) FeO content can be controlled more accurate ly by regulating the coke ratio in which the effect of free carbon content of raw materials is corrected. From those facts, the following measurement systems are developed. (1) Continuous FeO measurement meter for raw materials ----- The principle
of FeO measurement meter cons i sts in inductance change of detecting coil by the FeO content of raw materials. (2) Continuous FeO measurement meter for sintered products. (3) Particle distribution measurement system of c rush ed coke ----- This system uses an optical pattern recogni tion method. (4) Free carbon content measurement system of raw materials ----- This system estimates the total carbon consumption by calcu lating the data of flue gas vol ume and components. The recent operation has obtained the changing the desired value of RDI from 40% to 42% as a result of the improvemen t of con trol accuracy, so the FeO and Si0 content of products can be cut down more than 0.7% which bring 2 about much cost-down of products. Keywords Sintering plant; RDI; TI; Magnetite Me ter; Sintered Products; Raw Materials; Coke Breeze Particle Size Distribution; Free carbon content; Quality Control.
347
348
O. Arai et al .
INTRODUCTION The Sys t em adopted in the sin t ering plant a t Kashima is the DDC (Direct Digital Control) system which performs a series of process controls, from the raw materials weighing control to the burn through point control. That system has attained much improvement of the quality of sintered products and saveenergy by means of decreasing the coke rat io and the dispersion of RDI and basisity . One of the reasons of the stable operation of blast furnaces is well known to charge the high quality sintered products. Recently, moreover, operating conditions of blast furnaces are desired to make better and much more flexible, which make advanced quality control of sintered products necessary such as the quality indices of RDI, TI and basisity are measurable and controllable continuously. Under those backgrounds, SMI has developed quality measurement sensors and control system with satisfactory results. This paper presents an outline, with the results, of the quality measurement sensors and control system. EFFECTS OF CONVENTIONAL DDC SYSTEM In 1977 DDC system was developed, it's control systems are shown in Fig.l. The control models of this system were constructed based on the research made in the past several years at our central research laboratory and the analytical results of the micro-computer based data logging of sintering plant for about two years. Table 1 shows the process control items of DDC . The DDC system has brought us many effects shown in Table 2 . There installs an automatic calibration sub s ystem of Constant Feed \
where L
self inductance of iron core solenoid coil )le = effective permeability of iron core d diameter of solenoid coil 1 length of solenoid coil N turn of solenoid coil K Nagaoka's factor Y filling up rate of sintered products in solenoid coil FeO content in sintered products Feo Lo self inductance of coreless solenoid coil =
FeO content in sintered products is measured and calculated by the self inductance of solenoid coil which is filled up of sintered products . Self inductance is changeable not only FeO content but also filling up rate of solenoid coil mainly . So, in case of batch sampling and measurement system, samples are had to classify in proper particle size, but this method is not practical for having some of weak points written before . The indispensable conditions of Magnetite meter for quality control as our regards are listed below. (1) (2) (3) (4)
FeO content can be measured continuously. Filling up rate can be constant . Sampling system should be simple. Specimen should be sampled at the representative part of sintered products
Thus, optimum sampling and measurement system has been developed shown in Fig . 4. Fig . S shows the relation between Magnetite meter and FeO-chemical analysis. Fig . 6 shows the relation between FeO and RDI in sintered products. Those facts can be possible to control RDI of sintered products by using the Magnetite meter for the input value of feedback control system. This feedback control system has been effected to decrease the long-rangedispersion of RDI remarkably. But, there has been a limitation to control more accurately and quickly as it's long time delay, also two hours from raw materials feeders to the exit of the cooler. So, the next step system was designed consisting of the two control sub-systems written below. (1) Feedforward control system by which using the measurement of FeO content in raw materials. (2) Feedback control system by which using the measurement of FeO in sintered pro ducts. We call Magnetite meters for raw materials and sintered products as R-Magnetite meter and S- Magnetite meter. EFFECTS OF CONTINUOUS FeO MEASUREMENT METER FOR RAW MATERIALS R-Magnetite meter can't be consist of similar system of S- Magnetite meter as the raw materials contain much moisture .
The Quality Control System of Sintering Plant So, R-Magnetite meter should be designed to measure the raw materials' FeO content of the outside of detecting coil shown in Fig.7. The key point of development was how to improve the sensitivity of R-Magnetite meter. Vortex current loss caused by the protector -- austenite type stainless steel tube -could be cut small be thinning the thickness and cutting off the protector of useless part of strength. Sensitivity could be improved by cutting small of vortex current loss and increasing the turn of solenoid coil and stabilizing the amplifier characteristics depending on temperature-change. Specifications of both Magnetite meters are shown in Table 4 and Fig.8 shows the relation between R-Magnetite meter and FeOchemical analysis. Fig.9 shows the correspondence between Rand S-Magnetite meters in the sintering plant operation. Output values of both Magnetite meters are so similar that FeO content in sintered products can be controllable by feedforward and feedback control. So, the control test of FeO content was carried out shown in Fig. 10. Results of control actions are written below. (1) When decreasing the mixing percentage of high FeO content raw material from 4% to 0%, also both Magnetite meters' indications decrease. Calculated FeO change is 0.84% (based on the relation shown in Fig.8) and measured FeO change is 0.8%. (2) When increasing the mixing percentage of high FeO content raw material from 0% to 4% and decreasing the mixing percentage of coke breeze from 3.32% to 3.22%, R-Magnetite meter's indication increases, but S-Magne tite meter's indication doesn't change. Those facts have proved that FeO content in sintered products can be controlled by regulating the FeO and coke breeze contents in raw materials. There is a last improvement point in RMagnetite meter that the indication drift caused by the mixing of various types of FeO content materials. Magnetite meter's characteristics for various kinds of FeO content materials is shown in Fig.ll. EFFECTS OF PARTICLE SIZE MEASUREMENT SYSTEM OF CRUSHED COKE It has been cleared that the FeO content in sintered products can be controlled by regulating the FeO and coke breeze contents in raw materials written before. Moreover, we have yielded the facts by laboratory experiment and operation analysis of sintering plant written below. There are close relations between FeO, TI and coke content, and when operating the
349
same coke content, TI and RDI are dependent on coke breeze particle size distribution. The development of continuous type of particle size distribution measurement system was carried out based on the optical type experimental system reported previously. The development items for practical application are listed below. (1) Sampling system for optimum dryness control. (2) Optimum control of sampling volume to keep at constant rate of falling volume and thickness. (3) Optimum regulation between focus length of the camera and lower, upper range of measurable particle size. (4) Threshold level tuning method for image processing of proper particle size. (5) Control method of particle size distribution. The yielded development results are shown in Fig.12-Fig.15 and Table 5. (1) Configuration diagram of particle size distribution control is shown in Fig.12. (2) Particle size distribution measurement system is shown in Table 5. (3) Threshold level tuning method is shown in Fig. 14. (4) Particle size distribution measurement result is shown in Fig. 13. (5) The relation between charging volume for Rod Mill and particle size disbribution is shown in Fig. 15. RDI and TI have been stabilized by making use of particle distribution control system based on the relations shown in Fig.16 and Fig. 17. EFFECTS OF FREE CARBON CONTENT MEASUREMENT SYSTEM OF RAH MATERIALS The quality improvement of sintered products can be executed under making use of R- and S-Magnetite meter, and particle size distribution measurement system for coke breeze. But there has been a residual unknown change of FeO content in sintered products, which can't be presumed based on the informations of the known input data of FeO and Carbon contents in raw materials and operating conditions of sintering plant. Our raw materials are so consist of various kinds of materials, such as fine crushed ore and blast furnace dust and converter slug and so on, that the unmeasurable carbon input in raw materials except for the coke breeze make probably change the FeO content in sintered products. So, the total input carbon content has been presumed to depend on the principle written below. Fig.18 shows the principle of the presumption method of total carbon content in raw materials, and the calculation formula is shown in Formula (4). C=G(C0 +3!2CO-lOO(1-N /79»!22.4 x M (4) 2 2 where CO = CO percentage in main flue gas 2 2 of sintering plant
O. Arai et al.
350
co
CO percentage in main flue gas of sintering plant NZ percentage in main flue gas of slntering plant main flue gas (Nmtminute) total material charge (kg/minute)
Precise calculation process is shown in Appendix 1. Operating results are shown in Fig.19. There has been cleared that the FeO content in sintered products is stabilized by regulating the coke breeze content based on the relation between FeO (FeO in sintered products - FeO-in raw materials) and the total carbon presumption in raw materials shown in Fig.20. So, the dispersion of RDI is decreased shown in Fig.2l. CONCLUSION 1. Quality control sensors for sintering
plant have been developed written below (1) S-Magnetite meter (continuous FeO measurement meter for sintered products) (2) R-Magnetite meter (continuous FeO measurement meter for raw materials) (3) Measurement system for coke breeze particle size distribution . (4) The presumption system for total carbon content in raw materials. 2. The quality indices of RDI and TI in sintered products can be controlled fairly stable by making use of those sensors. 3. Objective RDI can be increased possible from 40% to 42%, moreover, improvement of blast furnace operation having been carried out at the same period make possible to cut down the FeO and Si0 2 contents about 0.7% (there are close relations between RDI, TI and FeO, Si0 2 contents in sintered products). So, the hot metal making cost is saved by 0.3%. REFERENCES 1. G Meunier: Metallurgical Reports C.N.R.M.
No.9, December 1966 2. Kawasaki Steel Corporation: No.52 Instrumentation Comittee of ISIJ, 1972 3. J. LUCKERS, G. MEUNIER: "Regulation automatique continue de la qualite d'un agglomere sur une bande industrielle", International Congree of Automation in Iron and Steel Horks, 1970
Appendix 1 Presumption of Free Carbon Content 1. Data from Exhaust Gas Composition (CO), (C02), (02) % Exhaust Gas Volume G Nm 3 /min.
i) Presumption of N2 Composition in Exhaust Gas (NZ) = 100 - {(CO)+(COZ)+(OZ)} (1) ii) Presumption of Exhaust Gas Volume from N2 Balance Exhaust Gas Volume/Air Volume (2) = K = 79/(N2) Z.Supposition of Reaction i) Carbonate Resolution MeC03 ) MeO + C02 ii) Carbon Combustion C + 1/202---> CO C + 0Z~C02 iii) Ore Reduction 3Fe203~2Fe304 + 1/202
(3)
(4 ) (5) (6)
3.Gas Balance i) Input Air Volume 100 (NZ) in 79 (7) (02) in = 21 (8) ii) Output Exhaust Gas Volume 100*K (9) (N2) out = 79 (02) out = 100*K'''(02) /100 = K"(02) (10) (COZ)out= K*(C02)= (C02)C+(C02)R (ll) (CO) out = K*(CO) = (CO)C (lZ) where (CO)R is COZ from Carbonate Resolution(3), (COZ)C is COZ from Carbon Combustion (4) and (CO)C is CO from Carbon Combustion (5), from Oz Balance (OZ) out can be expressed (OZ) out = (02) - (C02)C - 1/2(CO)C (13) and Increase of Gas Volume is 100*(K - 1) = (C02)R + 1/2(CO)C (14) from equation (1)~(14), we get (CO)C = K*(CO) in (15 ) (C02)R 100*(K - 1) - 1/2K*(CO) (16 ) (C02)C = (C02) out - (C02)R = K*(COZ)+1/2K*(CO)-100*{K-l) (17) (02)R = (02) - (02)out= (C02)+1/2(CO)C = K"(C02) +K1'(CO)-100*(K-l) (18) from equation (15)~(17), GCCO, GCCOZ and GR C0 2 can be expressed as GCCO =G*(CO)/lOO (Nm 3 /min.) (19) GCC02=G*{(COZ)+1/2(CO)-100*(1-1/K)}/100 (20) GR C02 =G*{100*(1-1/K)-1/2(CO)}/100 (21) where G is Exhaust Gas Volume (Nm 3 /min.) OUTPUT
INPUT
CO [rom Free Carbon
Carbon ill Dust
4. T. SHIRAIWA, Y. SAKAMOTO et.al .: "CONTINUOUS MEASUREMENT OF THE PARTICLE SIZE DISTRIBUTION OF RAW MATERIALS", Proceedings of the lMEKO MOSKOW, 1981
Sintering Coke
C02 from Free Carbon
Nachine
r-----~/ Catbonctte MeeO]
iii)
r-----.:'~~ --Loss
Presumptive of Free Carbon C in Raw Materials can be expressed as C (G CCD+GC C0 2)*12/22.4M G*{( C02)+3/2(CO)-100*(1-1/K)}/22.4M (ZZ)
G CO C
G CO, C
G CO, R
351
Th e Quality Control System of Sint e ring Pl a nt
r------------ - ------------- - l------ --...-_-_-_--....L_---.
....--_---.JfL...-_-_--....,- --- - - -- - - - -- --- -...-----..... :=1"-_---, Feeding control of sinter feed and
Moi sture
coke breeze etc.
of raw material
flit:: I :
~
: :! I
I
I ! '~L' l
I
I
I
Level cont rol
Den city control
Burning control
Damper control
Burn ing through
of raw material
of raw material
of furnace
of wind
pOint
______ ,
: :: L. ======';j : ------~:
I: ::I :
control
L ___ _ __ ,
: :
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t
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:
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:
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Coke,Lime Return
Slnter feed
_ ......_ _
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':
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II I
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I
TABLE 1 Control
, I
I
lI :lIq:
. Data
Preparation
of
Reports
~
Process Monitoring
:
feed
addifion control
TABL E 2
3. Level control
Effec ts of
of
hot metal1s
0 .063
0 .046
metal's
value of Si content In hOt metal blost
furnace
making
Man power savlflg for weigher calibration
slug
I
! I
~
Sensors for Qual ity Control
FeO
R - Magnetite meter
FeO content in
content In
Item
sintered row
products
materials breeze
materials
Specifica tion of
magnetite
me ter
DOG
Dispe rsion of basisity
meta l
I
Free carboo content presumption in ro w
0 .040
in hot
I
I
Carbon con te nt presumption system
0.055
slug
I
at Kashima steel works.
S - Magnetite meter
BefOfe Installation After Ins1110tioo
Man power saving for repon
I I
Crushed coke (before Rod Mill) and coke (offer Rod Mill) pa n icle size distribution
sintered products
Reduction of coke ra tio of
I I
I
Particle size distribution measurement syst em
Dispersion of bos isi ty in
Objective
I I
Measured
TABLE 4
in hot
I
Doe Effects
Item
SI content
I
I
I
· C. RT · Data logging . · Dai ly and monthly reports . · Automatic calibration of C. F. W. and belt weighers . · etc.
control
6. Burn through point control
Oisperslon of
I I I
fo r control
I Material
,
,
I
I I
VHl ~ _____ J
TABLE 3
2. Moisture
iI
:,
I I
Others
5 Charging density control
Process cont rol back up
Objective va lue of basisity
I
lL _ _ __________ ____________________ _ ___ ____ _ _ _ _____________ __ _
4. Permeability Control
. On-line data transmission
in
,
I
I I
Name
acquisition
: :
I
I
I I
I I I
DD C
Computer
I I I
I I
i ,
( Si nte ring Process Control System)
COOlputer for management
I
: I
system of sintering plant
Items of
I I I I
r--:~~=~~~~-_-_-_-_-~J I , ,I
I
Fig. 1 Control
I
I I
I
Neutron probe Level meter Flow meter Cylinder Permeability measure of raw material at charge side Thickness mea sure of raw material at charge side Orif ice Thermocouple for furna ce The r mocouple f or waste ga s at wi nd box Permeability measure at wind box
I
,
Detector
I. 2. 3. 4. 5. 6. 7 8. 9. 10.
I
I
! I::
Control valve Var iable - speed motor
,, : : :
I
: :
I 1
cont rol
i!
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,ll:~1Illlll~l~~~}t~A~~::':::fl"~"T1i I Water
boxes
1.23
1.25
0 .044
0 .032
050
045 L25kg/H -M Ton 1440 Mon hour J
120 tv1on -hour
Fa, ,aw materia ls
Item Diameter Detecting
coil
Length Turn
Frequency Current
Fa, sintered products
105 "
105 "
2001
200L
3000turn
300 Hz Under I OmA
IOOOtur n 1000Hz Under I 0 mA
O. Ar ai et al.
352
Coke and Row ROD
Mill
Sintering Machine
Materials Mixing
RDI T! FeO
Cooler
Coke breeze Particle size Distribution
GCi Gpi Hi GMi :
+
Controller Process Measurement system Control Model
Fe O, RDI, Tl Chemical Analysis
(T!, RDI, FeO) Desire d
FeO (RDI , TU
Objective Free Carbon Obj ective co ke particle size dist ribution
Desired RDI and Tl
Fig.2 Quality Control Configuration Flow
of
Sintering
Plant
Oscill a tor 44
o
* ~
o
cC
~ Q)
0 J!1 c
·in
s . 53
0
S 56 3
0
0
0
OOo~ O 0 o o
32
40 FeO In
Output ~
and block diagram
•
0
o
Fig.6
7.5
o
et:
FeO and filling up rate
Principle
0
Sensitivity
Measuring objects -Filling up in the solenoid coilalso contain FeO component Inductance
0
Zero point
Detecting Coi I
Adjuster
Fig.3
o CfJO o
Detector
Automatic Constant Voltage Uni t
0
dO o
E 40 E
of
Magnetite - meter
slnrered
50 products
FeO in sintered v.s. RDI
products
8
6 .5
.'.,. :
5.5
Screen
•
c 0
4.5
If 3.5 2.0
3.0
Magnetite
Fig5
4 .0 Meter
5.0
6.0
Va lue (%)
Magnetite meter value in sintered products
_ - - L _ L - - =_ _
GL + 200
v.s. FeO Fig 4
Construction of magnetite meter products
for sintered
The Quality Control System of Sin t ering Plant
353
6
Pipe for Protection (SUS 304)
~~~~~~-- ----- ITronSducer t ·-n--iTI Recorder
4 4 Output of Magnetite
Fig.7
Flg.8
Construc ti on of magnetite meter for raw materials
s - Magnetite
j
:" ,
" '\
Meter
( %)
Relationship between output of magnetite meter and FeO in raw ma terial s
meter
... ....
.,'
S - Magnet ite meter
.. I..' ', ~. \.: ...~ ,
...
.... :.
... .-.;
10' !
'".
~ I Hr
9' !
5' ,
Fig.9
3' ,
4' ,
Correspondence between S - and R - Magnetite meters
Fig 10
Cont rol te st of
FeO
conte nt
30 r------,r-----~----~
•• 2 3
~ !!'. 0
~
Dot No. I
.,
5
Ore Romerol Iron Sand PF. Peru Dried Oust Cake SF Corolrake
6 7 B
Sinfer Ore M .B R Converter Slug
9
Dust Pelle • BF Dust
2 . 4
20
4
~ s 0
~
•5
10
IOD
50
100
Fig II
Value of hand sc reen ing
--+-
Valu e of porticle
dlsfr ibut ion system
~
size measurement
.c
0>
~
o Our pur of Magnetite
--0--
80
2
5
Accumulotive
150
8
15 20
particle
size
distribut io n (m/m)
Meler
Measuring
Fig. 13
Relationship between ou tput of magnetite meter and FeO In materials
T I and ROl ConTrol
Obj ective
Objec :l ve
depe nd on co ke
TI
Re sult of particle
RDI
breeze distribullon*
*
Ref er to Fig 16 &. 17
value
Feeding Weighl
Object ive
Control UM
Cha ring Weight
Feed Feed coke siz e
for word and bac k control of breez partIcle distr ibution
Crushed co ke parti cle size dis tribution
Coke breeze particle sIze dis tribution -\~
Mea suremenT system of particle siz e distribution
Co ke breeze par ticle size di st ribution
Coke breeze
Fig. 12
Configuration diagram control
of particle size distribution
size
distributi on
O. Arai et a'l.
354
Brightness of the background
~ View of the Field
Improved le ve l
threshold
*
Threshold le vel (General moth od )
Mistaken to be particle Darkness region
Threshold
Fig. 14
Our Method
Particle
Geveral Method
metho d
tuning
level
Principle
Item
Parlicle size c an be calcu lated by re ckoning numbers of darkness image elements
Measuri ng range (diameter)
0.5-30 mm
O.I-lOmm
Freguency of image processing
3s
3s
Objective Moisture of coke
Under 3%
Under 3%
400
400
Numbers of image processin for distribution calculation
E~5r-------------------'
..s~
o Charging
size
Principle and Specifications of particle distribution measurement system
TABLE 5
78 ·
•• • •• ••• ••••
weight : 30 - 45 T/ H
•• • •• • • • •
76 -
"
74
•
•
;:
72
• • •
70
20
10
44
Fig.15
Crushed
D
.~
conveyor
_______ J Gas Composition
iCOI ,iCO,I ,(O, 1 Carr ie·r Gas Process Compute r
C ' G [CO + 3/ 2 CO - 100 ----------.------ --- , - _x_(_I '_N_I_7_9_1_1 1_2_2_A_ M_ _-.l
Fig.IS
56
52 size
under
60
I mm (%)
Flg.16 Relation between T 1 and coke breeze particle si ze
Character istics of Rod Mi"
(
48
Coke breeze porticle
Average particle Diameter (m/m) (Ch arge to the Rod Mill)
D
Printer
---- --
Presumption of Free Ca rbon in Raw Material s
Sca le
The Quality Control System of Sintering Plant
../
42
~
E E
'"
~.
38
•••• •• /
34
•
1;;
•
"0
C ::l
355
30
• ••• •••• • •
a 0::
26 48
44
52
56
particle size under
Coke breeze
60
I mm
(%)
Fig.17 Relation between RDI and coke breeze particle size 12
I
16 5 / 22 20
0
4
4
8
12
16 5 / 23 20
4
2.7
Presumptive
2.6
Content of
2 .5 Free Corbon (0;.)
2.4
Coke Content 3.0 (0;.) in Row Materials 2.9 Operation Guidance FeO
in
..
4.5 Sintered Products (0;.)
4.0 3.5 42
RDI
40
under
3mm
38
(%)
36
Fig. 19 '81 May
.,
0.6
~
'b
June
• • • • • • •• • • • • ••• • • ••• • • ••
0.8
0.4
,f
•
0.2
-
30
~ ~
u
~
~
'aO/II 'all TES T
20
0
, .:: ~
5.0
0' ~
10
~
0
a:
•
'0
24
'§ Q> a. Cl) i5
4 .0
c
0
•• 22
Results of Test
26
28
of Test
Presumpfive Free carbon COnTent in Row Materials (%)
(BL NO) 12 13 14 15
*6 FeO = (FeO in sintered products ) - (FeO in Raw Materials)
Fig 20 Presumptive Free Carbon Content in Raw Materials V.S llFeO
9
Fig.21
10
Results
'81 11 12 I
16 17
' - - - - - - - ', '-------'
2
345
of Dispersion (fV) of
7
6
R Dr